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Wow,  that looks great AND  expensive  :yeah:

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  • also went out with Tommy to suss out the timings for the ferry at Liverpool

  • found me spark; combination of things 1) couldn't get to fire manually off battery, so took off the caps and the spark was very weak. even though Dyna say it doesn't matter which way the connecti

  • Just done my cam cover in VHT crinkle finish   looks the dogs B  

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picked up the r6 shock from Kais today.

looks a nice job and he's put a 100nm/mm spring in. they said they'll set it up for me and will also redo the valving if its not enough.

 

anyway here's the shock

 

the chain rubbed on the gas reservoir so i had to do a bit of grinding. was a bit scary, but i took the plastic cap off and there's loads of room in there so its all done now

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well its more or less done, engine turns over and electrics seem to work.

 

couldn't really do that much today as it persisted it down. So next job is to prime the engine, run a temp fuel line and fire her up/balance the carbs

 

need to relocate the horn and do a bit of snagging and then tax her and  MOT is due end August.

drewpy, what you use to paint the engine and all those stuffs that get hot?

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drewpy, what you use to paint the engine and all those stuffs that get hot?

its called VHT (very high temperature) Paint the crinkle finish paint is from Frost £10 and I recommend PJ1 off ebay, its expensive but is the best finish out of all the paints and doesn't need a primer. bake it afterwards (or run engine) to cure it.

  • 2 weeks later...

How's it going Drew, have you got her mot'd yet? 

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PICTURES, PICTURES,PICTURES!!!!!!

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having the carbs pro cleaned, they must have had residue in storage so picking up friday and try again!

 

Pics to follow ;)

How's it going Drew?

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How's it going Drew?

its not!

got some running issues;

Starts quickly with no choke and then picks up all the cylinders but have to use 1/4 throttle to do this
high RPM when warmed
won't rev over 6k and makes a funny noise if I push the issue

spark plugs suggest rich mix before carbs rebuilt, no air leaks

I'm just wondering if the skimming has affected the running ie too high compression or I've mistakenly didn't do the valve timing correctly (checked and double checked through during install)

anyone comes across this or give me some pointers please?

 

had the carbs just rebuilt and setup by NRP so no issues there.

compression check next and probably recheck valve timing and gaps

 

might have to go on the tracker, which is running great :)

You've still got time, wish I could be more help but you know a hell of alot more than I do when it comes to this sort of thing, I'm shure you'll work it out

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Is it not worth a performance ig unit with all the other work done?

Seems a pretty common failure, the fact you have 2 spares speaks volumes.

 

I have to agree, with the carbs deemed as spot on then ig would give the black plugs firing way too early or late giving a bad sooty burn. Or even worse some firing early others late.

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Is it not worth a performance ig unit with all the other work done?

Seems a pretty common failure, the fact you have 2 spares speaks volumes.

 

I have to agree, with the carbs deemed as spot on then ig would give the black plugs firing way too early or late giving a bad sooty burn. Or even worse some firing early others late.

one was for the issue I was having last year and the second coz it was only £10.

 

pissing down tonight so couldn't do anything :(

I finally found a nos cdi for mine on ebay for the price of a secondhand one, good things come to those who wait!

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well I've finally sussed it. As usual it was a few things;

1) the exhaust cam was 1 tooth out
2) A few valve gaps were out of specs (poss due to the head bedding down)
3) re torqued the head down and it took another 1/2 turn to get the necessary torque

thanks for your input fellas!

 

it revs out and so much better :yay:

the engine is a '91 xj600 in an Fz600 chassis.
 
well I've finally sussed it. As usual it was a few things;
 
1) the exhaust cam was 1 tooth out
2) A few valve gaps were out of specs (poss due to the head bedding down)
3) re torqued the head down and it took another 1/2 turn to get the necessary torque
 
thanks for your input fellas!
the engine is a '91 xj600 in an Fz600 chassis.
 
well I've finally sussed it. As usual it was a few things;
 
1) the exhaust cam was 1 tooth out
2) A few valve gaps were out of specs (poss due to the head bedding down)
3) re torqued the head down and it took another 1/2 turn to get the necessary torque
 
thanks for your input fellas!
 

Well done Drew I knew you'd sort it

Edited by Tommy xs

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